Peking Paris Rally
|
![]() |
![]() |
|
![]() |
![]() |
![]() |
One of the last decisions we
faced was over which tyres to use, the basic options being between modern
low-profile “traction” forest tyres (such as Colway remoulds) and reinforced
high-profile van tyres. The 4.5“ original steel wheel is a bit special and
available rally tyre offer for such a narrow wheel is very limited. In the end
we opted for the latter ones, and chose a semi-steel radial light-truck Chinese
(!) tyre, size 185R15C (674 mm outside diameter) by Chengshan, with a nominal
standard load of 875 Kg each. These are the ones I will be testing this weekend.
The idea is to maximize ground clearance and puncture resistance, even allowing
for a relatively small traction on mud or loose gravel. I will report on test
conclusions.
I drove the car for the first
time over the weekend. The idea was to do as many miles as possible running-in
the engine and getting acquainted with the car handling. We adjusted the
rear suspension height with a full tank (80 liters) plus 120 Kg in the boot. I
did about 500 miles on tarmac and smooth gravel roads (no sump protection
fitted) and was reasonably pleased with the steering, the handling and the
brakes (no need to remove valve…). I was not too pleased with the engine and we
later decided to remove it and check a number of things. So the engine is out
and this may prevent me from doing another run next weekend…
I plan to attend the Magnette & Steam Event on April 7th , so only 3
weeks to go…
- After the engine problem I decided to add a rev counter and oil pressure, oil temperature and water temperature gauges. We produced an extra octagon-shaped veneered cluster (placed on top of the dash using the ashtray insert), where we put the rev counter in the middle and the oil pressure and oil temperature gauges on the sides. The water temperature gauge is now on the central panel (radio space) together with the petrol tank level gauge.
- The ignition switch and starter knob are now on the left of the heater controls, behind the roll cage vertical section;
- We also added an extra veneered panel underneath the dash to accommodate additional switches plus the windscreen water jet switch;
- We now have the two petrol pumps and the two coils switched on and off from the instrument panel;
- The roll cage is fully bolted and can be removed if required. The space between the cage and the body, both on the front vertical sections and on the top horizontal ones, allow them to be used as handles by the co-driver (can also be used by the driver, but his hands are usually busy grabbing something else…);
- We glued an aluminum foil-surfaced fire-retardant 5 mm foam inside the top to prevent the car from getting too hot in the sun (we also did the same inside the aluminum gearbox cover to minimize the heat from a different heat-source…);
- The manual fire extinguisher is on the floor in front of the co-driver’s seat.
- The automatic fire extinguisher tank is also on the floor but behind the co-driver’s seat. It is operated from a control box at the rear of the aluminum gearbox cover, under the hand brake lever. There are jets on both sides of the engine compartment and on both sides of the cabin;
- The two tyres have now been moved inside the car, horizontally behind the co-driver’s seat (the new wider tyres make it impossible to fit both in the trunk, and I did not want any more welding…).
- Wheel mud flaps are transparent…
- Co-driver foot rest has three foot-operated switches, two on the right (wiper plus water jets) and one on the left (horn).
- There are sockets on the engine compartment, trunk and dash to plug-in a torch, additional instruments, etc.
- I plan to plug a i-Pod into the driver/co-driver headphone communication system so that we can listen to music/radio whenever possible.
There will be a final round of pictures before the car departure Wed night, because we had a last minute change of front coils, shock absorbers and mounts to get an extra inch of ground clearance (every little mm helps…).
Last minute changes included a totally revised suspension
set-up (1 extra inch of ground clearance, different shocks front and rear,
etc.), new rear axle bearings and sealing, a larger sump protection and a new
location for the Brandz pulse sensor.
The Duraluminium sump protection is now much larger than anticipated. We put a
34 mm round bar across the two front eyelets and welded two front support mounts
on it. The protection is bolted at the rear and also in between front and rear.
I enclose a number of low-res pictures to illustrate this. We believe it will
prove sufficiently strong to withstand abuse as a “skid” platform… We also added
a small protection for the diff lower bolt at the rear.
The pulse sensor is now parallel to the car axis on the left front brake disc
assembly.
At the rear inside the car we loaded the two spare wheels, 3 boxes of spares,
the jack, sleeping tent and mattresses. All the rest went into the trunk. Not
too heavy and plenty of space left there for our two small bags…
After a frantic late evening work last night, the car was finally loaded to a trailer today and is now on its way to Calais! I will fly to the UK tomorrow, pick up the car in Calais and cross back the Channel tomorrow night, ready for the Magnettes & Steam meeting on Saturday.
When I collected the car at
These last minute changes had been:
- lightening a 1” thick prop-shaft spacer we had previously used without any problems;
- fitting the sump guard;
- a new exhaust mount support bracket;
- and new bearings and ring sealing on the rear axle.
I drove carefully to
Winchcombe and planned to look for the cause at the end of the meeting. During
the meeting I had a word with Paul Batho who very kindly volunteered to help me
look at the possible causes. We drove to his place and in succession removed
each one of the first three possible causes but were unable to identify the
cause for the vibration. Thank you Paul for a late Saturday afternoon’s work…
The only real alternative left was the prop-shaft itself. At about 9.30 pm we
called Doug Smith of MG Motorsport and I arranged to meet him next day (Easter
Sunday) at 2.30 pm. He had a new MGB prop-shaft, which was ½ inch too long and
required a bit of trimming on the splines end to make it work comfortably when
the rear axle bumps up and down. But it worked and the vibration was gone. Thank
you Doug.
Why this happened is not totally clear. There was now a “play” on one of the
prop-shaft U-joints. It is possible that the new suspension height had created a
new angle for the U-joints to operate and this may have exposed a problem that
went undetected before. Or it could just have deteriorated during the 2,000
miles or so I had driven so far.
So after 2 days of detective work we had solved the vibration “mystery”. I then
drove a few hundred miles more, collecting my wife from Heathrow Monday morning,
doing again (this time with her) the GPS training test I had done alone before
and then driving to Bury S. Edmonds to deliver the car to the shippers Tuesday
morning.
It is on its way to
1 -
2 - 3
- 4 - 5 -
6
|
|